OSF Drop Link Refitted |
Having retrieved the relevant vehicle information from Autodata, regarding pressures and torques, I then set about the removal, replacement and re-balancing accordingly, which went very well indeed. I cleaned up the hubs with a wire brush, applied a light coat of low fling lubricant and then re-fitted the NSF wheel and tyre. Andy had removed a drop link on the OSF so I was instructed to hold fire on that side. At this point Andy was required elsewhere and then left me with instructions for the careful refitting of the drop link OSF (due to the close proximity of currently rotating pulleys). Once fitted I was then able to re-attach the OSF road wheel, and then lower the beam jack, in order to torque both road wheels to manufacturer's specification.
New Oil Filter Installed |
I was also required to improvise a repair to a rear-end exhaust shroud, which had become completely detached, due to "rotting" around its' securing bolts. Notwithstanding liberal application of rust penertrator and brushing, two of the remaining five viable securing bolts sheared upon their tentative removal. Thankfully there is a very large tub of spare nuts, bolts and washers held within the Workshop, within which I managed to source 3 suitably over-sized washers to re-pin the shroud to a satisfactory standard. Satisfied so far, I then lowered the vehicle in order to refill with the Manufacturer's specified grade and quantity of engine oil, and then also removed and replaced the Air Filter accordingly.
Re-filling Engine Oil |
With the fresh oil in and level checked, I then conducted a start in order to allow the oil level to re-settle accordingly. I then switched off the engine and re-checked accordingly (including beneath for any leakage) - of which there was none currently apparent. I then topped up to 5.5 litres and moved swiftly on to the Air Filter, which went without a hitch. I then de-greased and cleaned off the engine top cover to ensure a "job done" finish (or so I thought)!
Air Filter Replacement |
After confirming all appeared "OK", I was asked to sit in the vehicle while it was raised higher, in order to re-run the engine upon re-fitment, which did "thankfully" prove to be OK. It was subsequently suggested that the level of contamination from the previous leakage (despite my best-est cleaning efforts), was probably the cause, as upon re-fitment all was indeed well, and was gracefully informed - "it could have happened to anyone" (Big inner sigh of relief)! With vehicle lowered I was then requested to reverse the vehicle to the entrance of the workshop in readiness for the customers' retrieval, upon his payment for services professionally rendered of course!
Wallet - "check", Mobile Phone - "check", E-Cig, fluid & Charger - "check", Specs & Case - "check", TNT Woolly Hat "check", off to work I went, departing at 1615 hrs, and still with a very Happy Friday feeling indeed! Thanks guys - brilliant blur of another day at AA Automotive!
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